The pilot stated that he departed the airport for the 15-minute skydiving flight with about 20
gallons of fuel onboard. After completing a jump run, he was returning to the airport and
maneuvered the airplane on final approach. When the airplane was about 3 miles from the
runway and about 1,200 feet above ground level, the engine experienced a partial loss of
power. The pilot configured the airplane for the best glide speed, and, shortly thereafter, the
engine quit producing any power. The airplane subsequently collided with trees in an orchard
about 600 yards from the approach end of the runway.
Tag: U.S.
The pilot stated that he departed the airport with six parachutists for a jump flight. As the
airplane approached 1,000 feet above ground level, he noticed that the airplane wasn’t
climbing. He checked the engine gauges and noticed that the engine analyzer was flashing
“CHT” and the cylinder head temperature was 454 degrees F. As the pilot pitched the nose
down and turned back to the airport, he heard a muffled “thud” sound and saw white smoke
pour from the engine. As he prepared for a forced landing, four of the parachutists jumped
from the airplane. The pilot then performed a forced landing in a field, coming to a stop near a
dirt berm. An examination revealed a hole in the engine crankcase, near the No. 4 cylinder.
Various pieces of metal, including part of a “quick oil drain plug” were found in the engine oil
sump. The No. 4 connecting rod journal appeared distorted and displayed extensive heat
signatures. The crankshaft journals on either side of the No. 4 rod journals did not appear to be
distorted or to contain the same heat signatures and were coated with engine oil. The rod and
crankshaft bearings were scored. The signatures on the engine were consistent with the loss of
lubricant to the No. 4 connecting rod journal. A reason for the loss of engine oil to the journal
was not found.
The pilot said that he normally flew the airplane with the fuel selector positioned to the right
main fuel tank during skydiving operations. However, on the day of the accident, maintenance
was performed on the airplane, and three engine run-ups were performed using the left main
fuel tank. The pilot ferried the airplane back to its home base uneventfully with the left main
fuel tank selected. Before the accident flight, the pilot verified that there was adequate fuel in
the right main fuel tank; however, he did not reposition the fuel selector to the right main fuel
tank. During climb, about 800 feet above ground level, the airplane experienced a total loss of
engine power. The pilot was unable to restart the engine and performed a forced landing.
Subsequent examination revealed that the airplane’s right main fuel tank had been
compromised and was leaking fuel, whereas the left main fuel tank was intact and devoid of
fuel. Additionally, data downloaded from the airplane’s engine monitor revealed that the
engine power loss was preceded by a loss of fuel flow. Postaccident examination did not reveal
any preimpact mechanical malfunctions or failures that would have precluded normal
operation.
The balloon pilot conducted multiple sport parachute flights throughout the day without
obtaining a weather briefing. A SIGMET for severe thunderstorms, hail, and cloud tops to
45,000 feet was in effect for the area surrounding the takeoff and accident sites. Shortly after
the balloon lifted off on the accident flight, the ground crew was advised of a severe storm
warning for the area and observed the storm on radar via their cellular telephones. The crew
contacted the pilot by radio to advise him that the storm was growing quickly. The pilot
informed the ground crew that he would attempt to climb over the storm but shortly thereafter
expressed doubts that the balloon would be able to rise over it.
The pilot stated that, before starting the engine by manually rotating the propeller, he set the
brakes, throttle, and trim. He exited the airplane and proceeded to rotate the propeller. When
the engine started, it went to full rpm, and the airplane started to move forward on the taxiway
at a high speed. The airplane veered off the taxiway and continued its high speed taxi until it
impacted a hangar door, damaging the engine, both wings, and the right main landing gear.
The pilot reported that he had not chocked the airplane and thought the brake was set. He
further reported there were no mechanical problems with the airplane.
Prior to the flight, the pilot fueled the airplane with 16 gallons of jet fuel. He planned to make two local flights carrying skydivers aloft. During the second skydiving flight, he delayed releasing the skydivers due to traffic in the area. As he turned the airplane back toward the drop zone, the airplane’s engine experienced a total loss of power.
The pilot reported that he was descending to land after his final flight of the day. The airplane was about 1,500 to 1,700 feet above ground level and about 1.25 miles from the airport when the engine lost total power. The pilot made an emergency landing to an open field, and the airplane sustained substantial damage to the fuselage.
The pilot stated that he was descending the airplane from an altitude of 8,000 feet after releasing skydivers. During the descent, at an altitude of about 3,000 feet, the airplane’s door opened and contacted the underside of the wing. The pilot slowed the airplane and attempted to close the door but noticed that the door had warped and that the window was missing.
While landing, the airplane touched down short of the runway, the left main landing gear impacted the edge of the runway and collapsed, and the airplane departed the edge of the runway into a culvert. The airplane’s left wing sustained substantial damage.
On August 9, 2011, about 1714 mountain daylight time, a Cessna 182, N8718T, landed in a field while on approach to Boulder Municipal Airport (KBDL). The aircraft was substantially damaged and came to rest after striking a tree on the north side of the field.
The pilot stated that he fueled the airplane for two flights with skydivers and thirty minutes of reserve fuel. He further stated that during the second approach he had to adjust his intended flight path for other airplane traffic. Then, as the pilot decreased the pitch of the airplane on final approach, the engine sputtered and lost power.
According to the pilot, as he taxied the airplane to the runway for takeoff, the left main landing gear collapsed. Examination revealed that the left main landing gear had fractured and completely separated from the airplane about 6 inches outboard of its attachment point at the airframe.
The pilot of the skydiving airplane was performing the first takeoff of the day, and he had just raised the landing gear when the airplane experienced a complete loss of power in one of its two engines. There was still runway remaining, and the pilot made the decision to abort the takeoff.
During takeoff the airplane, which was taking off for a parachute jump, collided with trees lining the side of the grass runway. The pilot said that a previous flight that day had been uneventful. During the accident takeoff he said he heard a “pop” at rotation and the airplane pulled to the left.
The pilot received an unsafe landing gear indication for the left main landing gear when he configured the airplane for landing. He cycled the gear and then attempted a manual extension, both without success. The pilot then completed the landing on the nose and right main landing gear. A post accident examination of the left main landing gear actuator revealed that the supports for the actuator bearings lacked lubrication and that the bearings displayed wear due to inadequate lubrication.
The pilot flew four skydiving flights without refueling. On the last flight, after the skydivers exited the airplane, the pilot initiated a descent and the airplane experienced a total loss of engine power. The pilot knew he could not make it back to the airport and made a forced landing to a gravel area.
The airplane had not been flown for about 5 months and the purpose of the accident flight was a maintenance test flight after both engines had been replaced with higher horsepower models. Witnesses observed the airplane depart and complete two uneventful touch-and-go landings. The airplane was then observed to be struggling to gain altitude and airspeed while maneuvering in the traffic pattern.
The flight departed to the east with four skydivers for a local jump. One witness stated that, immediately following the takeoff, about 200 feet above ground level, a “percussive” pop from the engine was heard. Two witnesses stated that the right wing dropped, and the airplane impacted the ground.
The airplane was departing for a skydiving flight. During rotation, the jump door opened, which was located on the right side of the airplane. The pilot said that he was not concerned with the door, which would not have critically impacted the airplane’s performance; however, an experienced parachutist attempted to secure the door to the point where he was partially outside of the airplane.
During flight at 10,000 feet above ground level, the engine began to vibrate and run rough. Shortly thereafter, a loud bang occurred and oil was present on the windscreen. The pilot attempted a forced landing, and during the forced landing, the airplane landed short of the runway and impacted a ditch.
The Beech King Air had undergone maintenance that included a landing gear disassembly and inspection in preparation for the airplane’s sale. Following the landing gear inspection, the left main landing gear strut was overfilled to an extension that exceeded maintenance specifications due to the strut not being able to maintain the manufacturer’s specified pressure/extension.
The pilot was departing from a soft, dry, 2,200-foot turf airfield using soft/short field procedures. After becoming airborne, the airplane settled back onto the runway, became airborne, and settled onto the runway a second time. At this time the right main wheel separated and the landing gear strut dug into the terrain spinning the airplane around and bringing it to an abrupt stop.
The airplane landed from a skydiving flight with a remaining passenger after three parachutists had jumped from the airplane. The engine was not shut down and the airplane was pointed toward the vehicle waiting for the passenger to deplane. When the passenger exited the airplane, a ground crewmember leaned toward the airplane to talk to the pilot while the passenger went around the right side of the airplane.
During a skydiving flight at approximately 14,000 feet, an instructor positioned himself at the door opening with his jump student nearby. The student inadvertently pulled the instructor’s reserve parachute D-ring, deploying the chute and pulling the instructor out of the airplane
The pilot stated that after the 20 skydivers left the airplane, he “descended and entered at a 45-degree angle for the downwind leg for landing on runway 08.” Once on the downwind leg of the traffic pattern, the pilot stated that the “windshield began fogging up.” The pilot decided to make a 360-degree turn to the right while he wiped the window with a rag.