Categories
2013 C-182 East Moriches Non-Fatal Non-Fatal Single-Engine NY Tail Strike

C-182D Non-Fatal East Moriches, NY May 17, 2013

According to the pilot, he leveled the airplane at 8,500 feet for a tandem skydive. When the instructor
exited the airplane, the nose pitched up, then the airplane pitched over into a right, descending turn. The
pilot assessed the situation and determined that the right horizontal stabilizer was bent. He later
determined that the instructor’s drogue chute became trapped under the flap handle, resulting in a
premature deployment of the parachute. The drogue chute then caught the horizontal stabilizer, resulting
in a 45-degree downward bend. The pilot reported no pre-impact mechanical malfunctions or failures
with the airplane that would have precluded normal operation.

Read the NTSB report.

Categories
2012 Collisions Other Ferry Georgetown Loss of Aircraft Control Non-Fatal Non-Fatal Single-Engine OH PC-6 Pilatus Porter

PC-6 Non-Fatal Georgetown, OH November 3, 2012

The commercial pilot said he applied full power to go around after a bounced landing. Torque
generated by the turboprop engine pulled the airplane to the right, and the pilot stated that he
was unable to arrest the turn. The airplane collided with trees, resulting in substantial damage
to the right wing, fuselage, vertical stabilizer, both horizontal stabilizers, and the rudder. The
pilot reported there were no mechanical malfunctions or failures with the airplane or engine
that would have precluded normal operation.

Read the NTSB report.

Categories
2012 C-208 Caravan Loss of Aircraft Control NC Non-Fatal Non-Fatal Single-Engine Raeford

C-208 Non-Fatal Raeford, NC August 18, 2012

According to the pilot, during the landing on a grassy area that was parallel to the paved
runway, the airplane touched down and impacted a ditch near an intersecting taxiway. The
airplane became airborne, touched down on the other side of the intersecting taxiway, bounced
again, and then landed hard on the nose gear, which resulted in substantial damage to the
fuselage and subsequent collapse of the nose landing gear. In a telephone interview, the pilot
stated that the ditch was about 200 feet from his initial touchdown point and that he regularly
lands on the grass, in the opposite direction, in order to minimize the wear on the main landing
gear tires. No preaccident mechanical malfunctions or failures were noted with the airplane
that would have precluded normal operation.

Read the NTSB report.

Categories
2012 C-208 Caravan CA Chula Vista Loss of Aircraft Control Non-Fatal Non-Fatal Single-Engine

C-208 Non-Fatal Chula Vista, CA August 6, 2012

The pilot said that, while on short final, the airplane experienced a sudden sink rate when the
wind changed from a head wind to calm conditions. He was unable to arrest the sink rate even
after power was applied because of the lag time for the airplane’s turbine engine to spool up.
The airplane landed hard short of the runway. Postaccident examination of the airplane
revealed that the left side of the fuselage was dented and wrinkled, and the left main landing
gear was bent inboard of the axle and was missing its brake assembly.

Read the NTSB report.

Categories
2012 C-182 KS Non-Fatal Non-Fatal Single-Engine Rose Hill Tail Strike

C-182D Non-Fatal Rose Hill, KS July 28, 2012

As a skydiver was exiting the airplane, his parachute inadvertently deployed and struck the
right horizontal stabilizer. He deployed his reserve parachute and landed without further
incident. After all the skydivers had exited the airplane, the pilot saw that the right horizontal
stabilizer and elevator were damaged. After an uneventful landing, postaccident examination
revealed the right stabilizer spar was bent.

Read the NTSB report.

Categories
2012 C-182 Farmingdale Fuel Exhaustion NJ Non-Fatal Non-Fatal Single-Engine

C-182A Non-Fatal Farmingdale, NJ July 21, 2012

The pilot was returning to the airport after dropping off parachutists at 9,000 feet. He said that
the flight lasted about 30 minutes, and as he turned onto final approach in the traffic pattern,
he pulled the throttle back, and the engine lost power. The pilot performed a forced landing in
a field, and the airplane struck some power poles lying on the ground, resulting in substantial
damage to the airframe. Postaccident examination of the airframe and engine revealed no
evidence of a mechanical malfunction or anomaly that would have precluded normal
operation. Only residual fuel was recovered from the wing tanks, and there was no fuel in the
line from the tanks to the engine. The pilot stated that he should have monitored his fuel
gauges more closely.

Read the NTSB report.

Categories
2012 C-182 Loss of Aircraft Control NJ Non-Fatal Non-Fatal Single-Engine Sussex

C-182A Non-Fatal Sussex, NJ June 28, 2012

The pilot reported that, during the final leg of the approach, the airplane was above the
intended approach path and speed. Over the threshold of the runway, the airplane encountered
a gust of wind. The pilot announced on the common traffic advisory frequency his intention to
perform a go-around maneuver. He was unable to perform the maneuver prior to the hard
landing; he then proceeded to overrun the runway and the airplane nosed over, which resulted
in substantial damage to the left wing. The pilot reported that there were no mechanical
malfunctions or failures with the airplane that would have precluded normal operation. The
recorded wind at the airport about the time of the accident was variable at 4 knots and for the
hour before and an hour after the accident the wind was recorded as calm.

Read the NTSB report.

Categories
2012 C-182 CA Fuel Exhaustion Non-Fatal Non-Fatal Single-Engine Watsonville

C-182 Non-Fatal Watsonville, CA June 24, 2012

The pilot stated that he departed the airport for the 15-minute skydiving flight with about 20
gallons of fuel onboard. After completing a jump run, he was returning to the airport and
maneuvered the airplane on final approach. When the airplane was about 3 miles from the
runway and about 1,200 feet above ground level, the engine experienced a partial loss of
power. The pilot configured the airplane for the best glide speed, and, shortly thereafter, the
engine quit producing any power. The airplane subsequently collided with trees in an orchard
about 600 yards from the approach end of the runway.

Read the NTSB report.

Categories
2012 C-U206 IA Mechanical Failure Non-Fatal Non-Fatal Single-Engine Winterset

C-U206 Non-Fatal Winterset, IA April 1, 2012

The pilot stated that he departed the airport with six parachutists for a jump flight. As the
airplane approached 1,000 feet above ground level, he noticed that the airplane wasn’t
climbing. He checked the engine gauges and noticed that the engine analyzer was flashing
“CHT” and the cylinder head temperature was 454 degrees F. As the pilot pitched the nose
down and turned back to the airport, he heard a muffled “thud” sound and saw white smoke
pour from the engine. As he prepared for a forced landing, four of the parachutists jumped
from the airplane. The pilot then performed a forced landing in a field, coming to a stop near a
dirt berm. An examination revealed a hole in the engine crankcase, near the No. 4 cylinder.
Various pieces of metal, including part of a “quick oil drain plug” were found in the engine oil
sump. The No. 4 connecting rod journal appeared distorted and displayed extensive heat
signatures. The crankshaft journals on either side of the No. 4 rod journals did not appear to be
distorted or to contain the same heat signatures and were coated with engine oil. The rod and
crankshaft bearings were scored. The signatures on the engine were consistent with the loss of
lubricant to the No. 4 connecting rod journal. A reason for the loss of engine oil to the journal
was not found.

Read the NTSB report.

Categories
2012 C-205 FL Fuel Starvation Lake Wales Mechanical Failure Non-Fatal Non-Fatal Single-Engine

C-205 Non-Fatal Lake Wales, FL March 31, 2012

The pilot said that he normally flew the airplane with the fuel selector positioned to the right
main fuel tank during skydiving operations. However, on the day of the accident, maintenance
was performed on the airplane, and three engine run-ups were performed using the left main
fuel tank. The pilot ferried the airplane back to its home base uneventfully with the left main
fuel tank selected. Before the accident flight, the pilot verified that there was adequate fuel in
the right main fuel tank; however, he did not reposition the fuel selector to the right main fuel
tank. During climb, about 800 feet above ground level, the airplane experienced a total loss of
engine power. The pilot was unable to restart the engine and performed a forced landing.
Subsequent examination revealed that the airplane’s right main fuel tank had been
compromised and was leaking fuel, whereas the left main fuel tank was intact and devoid of
fuel. Additionally, data downloaded from the airplane’s engine monitor revealed that the
engine power loss was preceded by a loss of fuel flow. Postaccident examination did not reveal
any preimpact mechanical malfunctions or failures that would have precluded normal
operation.

Read the NTSB report.

Categories
2012 C-182 Caldwell Collisions Other ID Loss of Aircraft Control Non-Fatal Non-Fatal Single-Engine

C-182 Non-Fatal Caldwell, ID March 14, 2012

The pilot stated that, before starting the engine by manually rotating the propeller, he set the
brakes, throttle, and trim. He exited the airplane and proceeded to rotate the propeller. When
the engine started, it went to full rpm, and the airplane started to move forward on the taxiway
at a high speed. The airplane veered off the taxiway and continued its high speed taxi until it
impacted a hangar door, damaging the engine, both wings, and the right main landing gear.
The pilot reported that he had not chocked the airplane and thought the brake was set. He
further reported there were no mechanical problems with the airplane.

Read the NTSB report.

Categories
2011 C-208 Caravan Fuel Exhaustion Mesquite Non-Fatal Non-Fatal Single-Engine NV

C-208 Non-Fatal Mesquite, NV December 17, 2011

Prior to the flight, the pilot fueled the airplane with 16 gallons of jet fuel. He planned to make two local flights carrying skydivers aloft. During the second skydiving flight, he delayed releasing the skydivers due to traffic in the area. As he turned the airplane back toward the drop zone, the airplane’s engine experienced a total loss of power.

Read the NTSB report…

Categories
2011 C-182 Fuel Exhaustion Non-Fatal Non-Fatal Single-Engine OK Skiatook

C-182A Non-Fatal Skiatook, OK October 12, 2011

The pilot reported that he was descending to land after his final flight of the day. The airplane was about 1,500 to 1,700 feet above ground level and about 1.25 miles from the airport when the engine lost total power. The pilot made an emergency landing to an open field, and the airplane sustained substantial damage to the fuselage.

Read the NTSB report

Categories
2011 C-182 Non-Fatal Non-Fatal Single-Engine Tail Strike VA Warrenton

C-182A Non-Fatal Warrenton, VA October 10, 2011

The pilot stated that he was descending the airplane from an altitude of 8,000 feet after releasing skydivers. During the descent, at an altitude of about 3,000 feet, the airplane’s door opened and contacted the underside of the wing. The pilot slowed the airplane and attempted to close the door but noticed that the door had warped and that the window was missing.

Read the NTSB report

Categories
2011 Boulder C-182 CO Non-Fatal Non-Fatal Single-Engine

C-182C Non-Fatal Boulder, CO August 9, 2011

On August 9, 2011, about 1714 mountain daylight time, a Cessna 182, N8718T, landed in a field while on approach to Boulder Municipal Airport (KBDL). The aircraft was substantially damaged and came to rest after striking a tree on the north side of the field.

Read the NTSB report…

Categories
2011 C-182 Dandridge Fuel Exhaustion Non-Fatal Non-Fatal Single-Engine TN

C-182 Non-Fatal Dandridge, TN July 30, 2011

The pilot stated that he fueled the airplane for two flights with skydivers and thirty minutes of reserve fuel. He further stated that during the second approach he had to adjust his intended flight path for other airplane traffic. Then, as the pilot decreased the pitch of the airplane on final approach, the engine sputtered and lost power.

Read the NTSB report…

Categories
2011 C-182 Mechanical Failure Non-Fatal Non-Fatal Single-Engine VA Warrenton

C-182F Non-Fatal Warrenton, VA June 23, 2011

According to the pilot, as he taxied the airplane to the runway for takeoff, the left main landing gear collapsed. Examination revealed that the left main landing gear had fractured and completely separated from the airplane about 6 inches outboard of its attachment point at the airframe.

Read the NTSB report…

Categories
2011 AK C-P206 Loss of Aircraft Control Non-Fatal Non-Fatal Single-Engine Wasilla

C-P206 Non-Fatal Wasilla, AK May 27, 2011

During takeoff the airplane, which was taking off for a parachute jump, collided with trees lining the side of the grass runway. The pilot said that a previous flight that day had been uneventful. During the accident takeoff he said he heard a “pop” at rotation and the airplane pulled to the left.

Read the NTSB report…

Categories
2011 C-182 Fuel Exhaustion Lesage Non-Fatal Non-Fatal Single-Engine WV

C-182A Non-Fatal Lesage, WV April 10, 2011

The pilot flew four skydiving flights without refueling. On the last flight, after the skydivers exited the airplane, the pilot initiated a descent and the airplane experienced a total loss of engine power. The pilot knew he could not make it back to the airport and made a forced landing to a gravel area.

Read the NTSB report…

Categories
2010 C-182 Mechanical Failure MO Mount Vernon Non-Fatal Non-Fatal Single-Engine

C-182G Non-Fatal Mount Vernon, MO March 18, 2010

During flight at 10,000 feet above ground level, the engine began to vibrate and run rough. Shortly thereafter, a loud bang occurred and oil was present on the windscreen. The pilot attempted a forced landing, and during the forced landing, the airplane landed short of the runway and impacted a ditch.

Read the NTSB report…

Categories
2009 C-182 Mechanical Failure NE Non-Fatal Non-Fatal Single-Engine Weeping Water

C-182H Non-Fatal Weeping Water, NE August 22, 2009

The pilot was departing from a soft, dry, 2,200-foot turf airfield using soft/short field procedures. After becoming airborne, the airplane settled back onto the runway, became airborne, and settled onto the runway a second time. At this time the right main wheel separated and the landing gear strut dug into the terrain spinning the airplane around and bringing it to an abrupt stop.

Read the NTSB report…

Categories
2009 C-182 Cado Mills Non-Fatal Non-Fatal Single-Engine Prop Strike TX

C-182B Non-Fatal Caddo Mills, TX August 15, 2009

The airplane landed from a skydiving flight with a remaining passenger after three parachutists had jumped from the airplane. The engine was not shut down and the airplane was pointed toward the vehicle waiting for the passenger to deplane. When the passenger exited the airplane, a ground crewmember leaned toward the airplane to talk to the pilot while the passenger went around the right side of the airplane.

Read the NTSB report…

Categories
2009 C-182 Non-Fatal Non-Fatal Single-Engine OK Skiatook

C-182A Non-Fatal Skiatook, OK May 23, 2009

The pilot stated that after departure and climbing to approximately 200 feet, the engine lost power and the airplane began to descend. During the forced landing the airplane struck a power line and impacted terrain resulting in substantial damage.

Read the NTSB report…

Categories
2009 C-182 Kalispell Mechanical Failure MT Non-Fatal Non-Fatal Single-Engine

C-182 Non-Fatal Kalispell, MT April 4, 2009

The airplane used for the skydiving operation was equipped with a foot step just above the right wheel, which the skydivers used to launch from the airplane. As the last of four skydivers stepped on the foot step, the right main landing gear fell away. The pilot reported that after he flew around for about 1 1/2 hours to burn off fuel, he intended to perform a low pass over the runway before coming around to land.

Read the NTSB report…

Categories
2008 C-208 Caravan FL Homestead Non-Fatal Non-Fatal Single-Engine Tail Strike

C-208 Caravan Non-Fatal Homestead, FL December 7, 2008

The flight was at 13,500 feet overhead the airport, preparing for the skydivers to jump. The pilot turned on the green light to initiate the jump. He then felt the aircraft shudder, but did not lose control of the airplane. After most of the jumpers had left the airplane, one of the skydivers came forward and notified the pilot of damage to the tail.

Read the NTSB report…