The airplane had not been flown for about 5 months and the purpose of the accident flight was a maintenance test flight after both engines had been replaced with higher horsepower models. Witnesses observed the airplane depart and complete two uneventful touch-and-go landings. The airplane was then observed to be struggling to gain altitude and airspeed while maneuvering in the traffic pattern.
Category: Severity
The flight departed to the east with four skydivers for a local jump. One witness stated that, immediately following the takeoff, about 200 feet above ground level, a “percussive” pop from the engine was heard. Two witnesses stated that the right wing dropped, and the airplane impacted the ground.
The airplane was departing for a skydiving flight. During rotation, the jump door opened, which was located on the right side of the airplane. The pilot said that he was not concerned with the door, which would not have critically impacted the airplane’s performance; however, an experienced parachutist attempted to secure the door to the point where he was partially outside of the airplane.
During flight at 10,000 feet above ground level, the engine began to vibrate and run rough. Shortly thereafter, a loud bang occurred and oil was present on the windscreen. The pilot attempted a forced landing, and during the forced landing, the airplane landed short of the runway and impacted a ditch.
The Beech King Air had undergone maintenance that included a landing gear disassembly and inspection in preparation for the airplane’s sale. Following the landing gear inspection, the left main landing gear strut was overfilled to an extension that exceeded maintenance specifications due to the strut not being able to maintain the manufacturer’s specified pressure/extension.
A Portuguese citizent, pretending to be a photographer, hijacked the aircraft.
The pilot was departing from a soft, dry, 2,200-foot turf airfield using soft/short field procedures. After becoming airborne, the airplane settled back onto the runway, became airborne, and settled onto the runway a second time. At this time the right main wheel separated and the landing gear strut dug into the terrain spinning the airplane around and bringing it to an abrupt stop.
The airplane landed from a skydiving flight with a remaining passenger after three parachutists had jumped from the airplane. The engine was not shut down and the airplane was pointed toward the vehicle waiting for the passenger to deplane. When the passenger exited the airplane, a ground crewmember leaned toward the airplane to talk to the pilot while the passenger went around the right side of the airplane.
During a skydiving flight at approximately 14,000 feet, an instructor positioned himself at the door opening with his jump student nearby. The student inadvertently pulled the instructor’s reserve parachute D-ring, deploying the chute and pulling the instructor out of the airplane
The CASA was on a paradropping flight when all 16 para’s were forced to jump off at an altitude of about 3000m. The CASA returned to Agen airfield, but control was lost and the aircraft crashed some 500m short of runway 11.
The pilot stated that after the 20 skydivers left the airplane, he “descended and entered at a 45-degree angle for the downwind leg for landing on runway 08.” Once on the downwind leg of the traffic pattern, the pilot stated that the “windshield began fogging up.” The pilot decided to make a 360-degree turn to the right while he wiped the window with a rag.
The pilot stated that after departure and climbing to approximately 200 feet, the engine lost power and the airplane began to descend. During the forced landing the airplane struck a power line and impacted terrain resulting in substantial damage.
The airplane used for the skydiving operation was equipped with a foot step just above the right wheel, which the skydivers used to launch from the airplane. As the last of four skydivers stepped on the foot step, the right main landing gear fell away. The pilot reported that after he flew around for about 1 1/2 hours to burn off fuel, he intended to perform a low pass over the runway before coming around to land.
The non-instrument rated private pilot planned to attend a skydiving event near the destination airport that began the next day. Prior to departure, the pilot was aware of the low clouds affecting the destination airport. The pilot told an acquaintance at the destination airport that he needed to make the flight that night because of deteriorating weather conditions that were expected on the next day.
The flight was at 13,500 feet overhead the airport, preparing for the skydivers to jump. The pilot turned on the green light to initiate the jump. He then felt the aircraft shudder, but did not lose control of the airplane. After most of the jumpers had left the airplane, one of the skydivers came forward and notified the pilot of damage to the tail.
The pilot of a Piper L-4 airplane reported that shortly after he started the taxi roll from the parking area, he initiated a shallow turn toward the taxiway. As he reached the taxiway he steered to follow the centerline, however, the airplane continued to turn to the right. He reported, in part, that the left brake inputs were not responsive and the airplane continued to the right and collided with a standing occupied Cessna.
The private pilot stated that he was at an altitude of 3,500 feet when the engine stopped producing power. He made a forced landing to field and struck a cedar post with the airplane’s nose wheel and subsequently flipped over resulting in structural damage to the vertical stabilizer
The airplane was fueled before the pilot’s first flight that day. A total of 6.0 gallons of fuel were added to each fuel tank. After fueling, the pilot dipped each fuel tank using the provided dipstick, and determined that each tank contained between 7.0 and 7.5 gallons of usable fuel. He then flew one load of skydivers, returned, and attempted to secure the engine for fueling but was pressured by company personnel that he had enough fuel to make the second flight and that he needed to keep the airplane operating.
The helicopter impacted unmarked power transmission lines as the pilot maneuvered at a low altitude over a river. The helicopter impacted the river and separated into several pieces. The pilot and his passengers were not injured and were rescued by nearby boaters.
The pilot flew nine skydiving flights on the day of the accident in the Cessna 182A. Each flight was approximately 30 minutes in duration. The airplane was refueled after approximately every other flight with about 12 gallons of fuel. Prior to takeoff for the tenth and final flight of the day, the pilot thought he had about 16 gallons of fuel in the airplane; however, he did not visually confirm how much fuel was in the tanks and could not remember what the fuel gauges indicated.
Beach 90 King Air Non-Fatal Pitts Meadow, Canada August 3, 2008
The pilot reported that there were no observed anomalies with the left wing prior to the flight. During the flight, which was conducted as a local parachute operation, the pilot performed a descending turn. The left wing’s aileron bound when the pilot attempted to level the bank. The pilot declared an emergency.
The commercial pilot reported that he was en route to a parachutist jump zone on the first of two planned jumps. Prior to the first jump, before he had slowed the airplane, or illuminated the green jump light, indicating that the parachutists had permission to jump, two of the parachutists prematurely jumped.
The pilot landed on runway 33, which is a dirt runway. The wind direction at the time was 320 degrees at 19 knots, gusting to 29. The pilot turned the airplane around to back taxi to parking. While back taxiing, the airplane’s nose wheel encountered a soft spot of sand, and the pilot added some power to get through the soft spot. The tail came up, and the airplane nosed over.
The pilot reported that the airplane, which was used for sky diving operations, was climbing through 7,000 feet mean sea level (msl) when he heard an explosion followed by a metal grinding noise coming from the engine section of the airplane. He felt the airplane vibrate, and smoke began to fill the cabin. He reported that the engine was not producing any power so he shut the fuel off and performed procedures to rid the cabin of smoke.