According to the pilot, he completed an air drop of skydivers and was returning to land. During the final approach, he added power to maintain altitude and obstacle clearance, and the engine “quit without sputter[ing].” He made a forced landing in a sagebrush covered field. The airplane struck the ground, slid down a gully, and struck a tree.
Category: C-182
The airplane landed downwind, approximately halfway down the runway, overran the end of the runway and nosed over. The pilot reported that while en route he monitored a nearby automated weather observing system (AWOS) and the winds were “230 [degrees true] at 3 knots.” The pilot stated, “I decided I would use either end of [the] runway since [the] wind was calm.”
The 363-hour single-engine commercial rated pilot lost control of the airplane during a parachute activity flight. The airplane subsequently stalled and entered a spin to the left. A witness radioed the pilot and asked what was wrong, and the pilot replied that he was in a spin and didn’t know what to do.
The commercial pilot reported a partial loss of engine power during takeoff. He was unable to restore full power, and made an emergency off-airport landing, which resulted in structural damage to the airplane. An FAA inspector and an aviation mechanic examined the engine and noted that the gasket between the air filter and carburetor was missing.
A witness reported that the airplane touched down within 1,000 feet of the runway threshold. The airplane rolled about 200 feet, and the nose gear collapsed. The airplane then veered left and came to rest inverted. The witness added that the nose gear collapse left scrape marks on the runway. Examination of the airplane revealed that the upper link of the nose gear torque knee had failed.
Approximately 1 hour into flight, the engine lost all power, and the pilot attempted a forced landing to a field. During the landing, the airplane struck a tree located at the approach end of the field. The pilot initially reported that he departed with 2 inches of fuel in each tank, with the intention of flying 1 hour.
While the aircraft was level at 10,500 feet above sea level (MSL), four skydivers took their positions on the right exterior jump-step of the aircraft. Just after the last jumper was on the step, the parachute of one of the jumpers inadvertently deployed and streamed back into the aircraft’s tail surfaces.
The pilot made a hard landing collapsing the nose gear and damaging the firewall. The pilot took off and turned to downwind for landing. He reported that he flew an uneventful and normal approach. He said that he touched down on the main landing gear, but the nose gear folded under the airplane as it touched down.
The pilot stated that he had recently purchased the airplane in Deland, Florida, and was ferrying it to Southeast Greensboro Airport, Greensboro, North Carolina. He said that he was enroute to the Siler City Municipal Airport, Siler City, North Carolina, for a scheduled fuel stop, and was approaching the airport at an altitude of about 5,500 feet, when the engine ceased operating.
After the parachutists jumped, the airplane was descending through 9,000 feet msl, and the engine lost partial power. The pilot verified that carburetor heat was on, the cowl flaps were closed, the fuel selector was positioned to “Both,” and the mixture was rich. She continued descending and entered a left traffic pattern for the runway. The pilot initially judged her pattern distance based on the available engine power.
While landing on runway 3, the airplane’s right wing contacted the runway and the airplane landed hard. A weather observation reported at an airport about 18 miles northeast of the accident site, included winds from 320 degrees at 13 knots. The pilot further reported that he conducted an uneventful flight an hour prior to the accident, with the same wind conditions.
The airplane initiated a forced landing after a partial loss of engine power during the takeoff initial climb. During the initial run-up the magneto check was not within acceptable limits; however, approximately 15 minutes later the pilot rechecked the magnetos and they were within acceptable limits. The pilot said he configured and checked the airplane prior to takeoff with 10 degrees of flaps and all gages “in the green.”
The pilot landed long beyond his intended touchdown point. He delayed his decision to initiate a go-around. The airplane struck trees at the end of the runway.
After releasing parachutists, the pilot planned to return to the airport. During the descent, about 2,500 feet msl, the engine began to lose power. The pilot thought that carburetor ice caused the power loss, and performed emergency procedures, which included the application of carburetor heat. The engine did not regain power, and the pilot planned an emergency landing to a field.
On the fourth parachute drop flight of the day for the pilot and aircraft, the pilot detected a reduction in elevator control authority on takeoff. He elected to continue the takeoff and climbed to 3,500 feet agl, where he released the two parachutists. On return to the airport, he used power to control his flare, but landed hard and began a porpoise maneuver.
A US Army Pilatus UV-20A collided in midair with a Cessna 182C during parachute jumping operations. The collision occurred about 4,800 feet msl (2,800 feet agl) on the northeast side of runway 12 abeam the approach end. Both aircraft had made multiple flights taking jumpers aloft prior to the accident. The Pilatus departed runway 12 about 5 minutes prior to the Cessna’s departure on the same runway.
After the pilot dispatched two parachutists, the pilot commenced his descent to return to the airport. While on final approach, approximately 200 feet AGL, the engine lost power. The pilot attempted to land in a nearby open field rather than to attempt maneuvering around high power lines near the airport.
The certificated commercial pilot was conducting skydiving operations in the vicinity of the accident airport. After the airplane climbed to about 11,500 feet msl, all three of the skydivers aboard exited the airplane, and the pilot began a descent to return to the departure airport. The pilot said that while on approach, all engine power was lost, and emergency engine procedures did not restore engine power.
After the sky divers exited the airplane at 12,000 feet, the engine lost power while the airplane was descending through 10,000 feet. The pilot switched fuel tanks and engine power was reestablished. The engine again lost power at 4,000 feet and the pilot attempted a forced landing at his home base airport.
The pilot stated that as the aircraft descended, the engine was operating at 2000 rpm, and the selected manifold pressure was 15 in Hg, and at 8,000 feet he noticed that the engine had ceased operating. Prior to noticing that the engine had ceased operating he said everything had been normal, but as he maneuvered to land he felt he was too far down the runway to land safely, so he elected to perform a go-around.
The airplane nosed over in a cornfield during a forced landing after a total loss of engine power. The pilot reported he released the parachutists at 10,100 feet msl over the drop zone and started the descent to the south due to better cloud clearances and to keep clear of company traffic. He reported that he applied carburetor heat before descending.
The pilot of the skydiver dropping aircraft reported that the engine lost power at the end of his descent from the 12,000-foot drop altitude as the airplane approached a landing 3-mile base leg. When the engine lost power, he checked that the fuel selector was in the “both” tanks position, the mixture was in the “rich” position, and checked individual magnetos; all with no effect.
The flight departed with approximately 20 gallons of fuel in each fuel tank and offloaded skydivers at 10,500 feet, then descended to return with the throttle at idle, the fuel/air ratio leaned; and carburetor heat applied. At 2,000 feet, the pilot began to level off and, “realized I was having engine trouble and began my emergency procedures for an engine failure at altitude….”
After discharging three parachutists into a drop zone from about 12,000 feet mean sea level, the pilot attempted to return to the departure airport. The engine began surging as the airplane descended through 8,000 feet. The pilot continued the descent and entered the departure airport’s traffic pattern. He misjudged his distance from the runway, and when all engine power was lost turning onto the final approach leg he was unable to glide to the runway.
The pilot reported that she taxied the aircraft to the grass covered run-up area in preparation for takeoff. As the aircraft moved over the grass, a ‘snapping’ sound was heard and the aircraft ’tilted back and to the right.’ The right wing and right side stabilizer contacted the ground.