Following the 12th sport parachute jump of the day, which occurred after sunset, ground witnesses observed the airplane descend into the ocean in a left wing low, nose down attitude. They did not hear the engines sputtering or popping, or see the airplane make any erratic movements during its descent.
Category: 1
According to the FAA, the skydiver was standing on the strut preparing to jump when his pilot parachute opened and wrapped around the tail section of the airplane.
During the loading of 17 parachutists, a 31-year-old male parachutist notified the loader/jump master that on his next jump he would have a smoke canister on the airplane and that the pilot should be notified.
The flight returned from dropping parachutists, and the pilot left the engines running as the next load of parachutists loaded. A passenger, who had ridden on the previous flight, was instructed by the pilot to exit through the rear door and that ground personnel would direct her.
The pilot stated that after climbing to 10,000′ msl on a skydiving flight, the occupants began preparations for the fourth and final parachute jump of the day. The first parachutist (skydiver) of three was standing on the right wing strut preparing to jump, when his main parachute (that he had packed himself) deployed inadvertently.
During an attempted freestyle jump from 10,500 feet msl, the parachutist gripped a bar in the airplane, then swung his legs outside and let go. During this attempted exit, the parachutist hit his head on the doorway floor.
A piper pa-28, n3011f, was in vfr cruise flight heading eastbound at about 5700′ msl, as a cessna 210 (parachute jump plane) had just completed a clearing turn to a westbound heading, into the sun, at 7300′ msl. A parachutist jumped from the jump plane & struck the vertical stabilizer of the pa-28 after a few seconds of free fall. Control of the pa-28 was lost, & it crashed in an uncontrolled descent.
The reserve parachute of one of the skydivers inadvertently deployed and pulled him out of the airplane, striking the left horizontal stabilizer. Examination of the reserve parachute revealed no evidence of any fault with the automatic signaling device.
The passengers(parachutists) reported that after the airplane became airborne they heard ‘backfiring’, a ‘bang’ and ‘….Saw white smoke…’ the jumpmaster reported that the engine quit after the airplane turned downwind. The airplane continued to lose altitude on downwind and during the turn to the runway. It crossed the approach end of the runway at a 45-deg angle and dragged a wing on the runway, coming to rest next to the runway.
The pilot had taken a newlywed couple up on a ceremonial ‘mile high’ local pleasure flight as a wedding gift. He reported that during a maneuver he felt a ‘shudder’, and elected to make a low pass over an airport taxiway, by some friends on the ground with a hand-held radio, for a ‘landing gear check’. During the second pass the pilot asked the couple to ‘look to the right where the moon shines over barnwell.’ the airplane collided with a spectator on the taxiway. A pax stated that the pilot then ‘freaked out’ and was in no condition to fly the airplane. During a subsequent landing attempt, a pax prevented a go-around by forcing the yoke forward and pushing on the brake pedals with his hands. The pax stated the pilot ‘wanted to keep flying and he was going nuts.’ the pilot fled the scene after the accident but returned later. The pilot had arranged to have the people on the ground ‘moon’ the airplane during the low pass.
The flight was in level cruise and 3 of the 4 jumpers were positioned on the step ready to jump. The reserve chute on one of the jumpers accidently deployed and was sucked forward and over the right wing leading edge. The jumper was pulled forward and over the wing, and in the process, hit his head on the wing leading edge and substantially damaged the internal wing structure. As the jumper’s chute deployed over the wing, the aircraft was rolled inverted. The other jumpers jumped and parachuted to the ground safely.
During a skydiving operation, the aircraft was slowed to slow cruise flight for a parachute jump. As skydivers were moving to the exit door for a group jump, the d-ring of one skydiver’s reserve parachute became entangled on a protruding cabin door support bracket. The reserve chute deployed & was caught in the slip stream. The skydiver was then pulled from the open door. He impacted the right horizontal stabilizer, fell 4000 ft to the ground & was fatally injured. Most of the right stabilizer was torn from the aircraft. After its separation, the aircraft entered a dive & the remaining skydivers jumped from the plane.
After dropping skydivers the pilot entered a descent to return to the airport for another load of jumpers. He was receiving radar advisories during the drop from a tracon controller. As the aircraft descended below 4,000 feet msl the controller terminated the radar advisory service. Immediately after the controller discontinued the service he asked the pilot to check for a stuck microphone switch. The aircraft continued its descent and collided with a camping trailer and building under construction in an extreme nose low attitude. The elevator trim was found in the full nose down position. No other malfunctions were found.
The non-instrument rated plt was on a flt to psn the acft for sky diving activities. As he was transiting the albany arpt radar svc area at 5500′, radio and radar ctc were lost. Subsequently, the acft crashed in a steep dive and was demolished by impact. Psnl in the area rprtd an ovc cond and estd the vis was at least 1 mi. Abt 12 mi ese, the 0750 albany wx was in part: 1200′ sct, 6000′ bkn. Vis 2 mi with fog. Low clouds at the rprtg stn had lifted by the time of the acdnt.
After dropping the parachutist, the acft was observed to fly eastward over the dz, make a left 180 turn, line up on the parked van on an easterly heading and descend to a low altiude. Witnesses estimated the altitude at from 10 t0 30 ft agl. The van was parked on a ridge across the flt path. The acft made a low alt-high speed run toward the van. Just before striking the van with the ldg gear, the acft seemed to duck under a low power line in its path.
The acft was on a parachute jumping mission. After climbing to 9000 ft msl, 4 sky divers jumped out & the plt began a descent back to the arpt. The acft was seen level at aprx 500 ft agl & in the aprx position for a downwind leg for a left pattern for runway 36. About 1/2 mi north of the normal turn point for the base leg, the acft began a steep descending left turn. Witnesses described a bank angle of 45 to 75 deg & a nose down attitude of 20 to 30 deg. One of the witnesses reported that the bank and descent angles then began to decrease, but at impact, the nose was still low & the bank angle was about 20 deg. Observers saw no indication of plt control movement before impact. An exam of the wreckage revealed no evidence of an inflt failure/malfunction. The plt’s wife said that onoccasions, he had experienced severe headaches, but never to an alarming point. She reported that he took only asprin for the headaches. Pathological & toxicological exams reflected no evidence of a preimpact incapactiating problem.
Three observers accompanied the aircrew & other passengers on a flt to transport skydivers aloft. Prior to the flt, all 3 of the observers were briefed not to exit the acft until the engines were secured. However, 1 of the 3 discussed the need to move a cessna 172 at the completion of the flt. After returning from the flt, the aircrew stopped the plane on the ramp. While the engines were still running, the occupant that wanted to move the cessna exited the acft. Unbeknown to him & the plt, the other 2 occupants also exited the acft. One of them walked into the arc of the left propeller & received a fatal head injury.