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1996 C-182 Loss of Aircraft Control Non-Fatal Non-Fatal Single-Engine

C-182 Non-Fatal Crestview, FL June 6, 1996

The pilot stated that he elected to land to the south on the 1,600-foot grass runway due to the prevailing winds at the departure airport and he had never landed at the airstrip before. He entered the pattern to land and with full flaps extended, the airplane touched down hard on the nose landing gear, bounced, then touched down and nosed over.

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1996 C-P206 Non-Fatal Non-Fatal Single-Engine Tail Strike

C-P206 Non-Fatal Goshen, IN May 26, 1996

During a parachute jump activity one of the two parachutists on the airplane’s jump step began a cadence used to jump from the step. According to the jumpmaster the parachutist began an exaggerated rocking motion. During this rocking motion his reserve parachute’s ripcord pin protective flap brushed against the airplane’s open door.

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1995 C-182 Non-Fatal Non-Fatal Single-Engine Undetermined

C-182 Non-Fatal Walworth, WI September 3, 1995

The pilot reported that climbing through 550 feet agl, the engine lost power. He lowered the nose of the airplane, established a glide, checked the engine controls and fuel selector, and pulled the carburetor heat control to no avail. At one point, ‘the engine started but would run at a fast idle, and for only a few seconds.’ he conducted a forced landing in a soybean field. Examination of the wreckage revealed no anomalies. During a test in a production test cell, the engine operated normally and produced maximum rated power.

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1995 C-182 Non-Fatal Non-Fatal Single-Engine Preflight

C-182 Non-Fatal Derby, KS July 15, 1995

The pilot reported that after the airplane reached an altitude of 10,500 feet msl, the skydivers exited the airplane. The pilot stated that he then began a wings-level, high-rate descent to stay clear of the drop zone. The mixture was at full rich and the carburetor heat was applied as he maintained 150 to 160 knots indicated airspeed.

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1995 C-180 Non-Fatal Non-Fatal Single-Engine Preflight

C-180 Non-Fatal Springdale, AR July 4, 1995

The pilot lost control of the tailwheel equipped airplane while attempting to land on runway 18 with a crosswind from 290 at 19 knots, gusting to 37. The airplane ground looped and the left wing spar was damaged when the wing impacted the ground.

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1995 C-182 Collisions Other Non-Fatal Non-Fatal Single-Engine

C-182 Non-Fatal Paso Robles, CA June 17, 1995

Two airplanes were converging head-on while taxiing on the same east-west taxiway. The pilot of the cessna 182 was taxiing east and saw the tailwheel equipped great lakes 2t-1ak (biplane) ‘s-turning’ on the taxiway. She assumed the biplane pilot saw her aircraft.

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1995 Helio H-250 Mechanical Failure Non-Fatal Non-Fatal Single-Engine

Helio H-250 Non-Fatal Clarkson, NY May 18, 1995

The pilot departed on a local flight with three passengers. The engine start, taxi, and initial takeoff were normal. As the airplane flew over the end of the runway at 50 to 75 feet, the engine lost power.

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1995 C-182 Fuel Exhaustion Non-Fatal Non-Fatal Single-Engine

C-182 Non-Fatal Bowling Green, MO March 11, 1995

The airplane was descending for a landing when the engine suffered a total loss of power. The pilot stated that he had no memory of the accident. Although personnel who moved the airplane claimed that 15 or 16 gallons of fuel were removed from the accident airplane at the accident scene, only about six gallons could be located.

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1994 C-182 Non-Fatal Non-Fatal Single-Engine Tail Strike

C-182 Non-Fatal Bowling Green, MO December 17, 1994

The airplane took off with four parachutists on board. After reaching an altitude of 11,000 feet, one parachutist exited the airplane. As the second parachutist was exiting, his reserve parachute deployed pulling him toward the rear of the airplane. The parachute canopy went over the top of the horizontal stabilizer and the parachutist went under the stabilizer.

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1994 C-182 Mechanical Failure Non-Fatal Non-Fatal Single-Engine

C-182 Non-Fatal Worthington, PA Oct. 15, 1994

The pilot was returning from a skydiving drop when he entered the airport traffic pattern, experienced an inflight loss of control, and then struck trees short of the runway.

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1994 C-182 Engine Failure Fuel Contamination NC Non-Fatal Non-Fatal Single-Engine Preflight Raeford

C-182 Non-Fatal Raeford, NC July 19, 1994

AFTER FUELING THE AIRCRAFT, THE PILOT OBSERVED ‘A LOT’ OF WATER IN THE FUEL, WHEN CHECKING THE SUMPS. HE SHOOK THE WINGS, AND AGAIN OBSERVED WATER. HE ALLOWED THE AIRCRAFT TO SIT FOR ABOUT AN HOUR, THEN HE CHECKED THE SUMPS AGAIN. HE DRAINED WATER UNTIL NO MORE WATER WAS OBSERVED. AT ABOUT 200 FEET AGL, DURING THE INITIAL CLIMB, THE ENGINE QUIT.

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1994 Improper/Poor Maintenance Non-Fatal Non-Fatal Single-Engine PC-6 Pilatus Porter

PC-6 Porter Non-Fatal Raeford, NC July 9, 1994

The pilot was performing the initial takeoff, when he observed a loss of power, associated with a torque indication of zero. He force landed the aircraft in a wooded area when he could not make an open field. A post accident inspection of the engine revealed that the fuel control unit arm was loose, and the lock wire was not in place.

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1994 C-182 Loss of Aircraft Control Non-Fatal Non-Fatal Single-Engine

C-182 Non-Fatal Glencoe, MN May 22, 1994

The 81-year-old pilot was flying to the glencoe municipal airport to pick up parachutists. The glencoe airport has a grass runway. The pilot landed in a grass field one-half mile south of the airport. Witnesses reported the pilot circled the field before landing. The airplane struck a fence post and nosed over during landing roll.

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1994 C-182 Fuel Exhaustion Non-Fatal Non-Fatal Single-Engine

C-182 Non-Fatal Bryan, TX May 21, 1994

On final approach to runway 14, a total loss of engine power occurred. Due to construction equipment, transmission lines, and vehicle traffic on a highway, the pilot made a decision to land in a field. During the landing in rough and uneven terrain, the nose gear, left main gear, and left wing were damaged. The pilot reported 15 gallons of fuel at the initial preflight.

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1994 C-182 Non-Fatal Non-Fatal Single-Engine Tail Strike

C-182 Non-Fatal Ellejay, GA April 30, 1994

A student sport parachutist was preparing for a static line jump. The parachute inadvertently deployed as he was moving into jump position, outside of the airplane. Canopy static lines caught on the horizontal stabilizer, twisting the empennage.

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1994 C-170 Mechanical Failure Non-Fatal Non-Fatal Single-Engine

C-170 Non-Fatal Bushnell, FL April 26, 1994

The commercial pilot was about 50 feet agl on initial takeoff climb when the airplane started to vibrate and the engine started running rough. The pilot determined that he could not clear trees at the end of an open field and made a forced landing straight ahead maneuvering around some trees and cattle. The pilot stated he flared a little high, landed hard and the right main landing gear separated.

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1994 C-208 Caravan Loss of Aircraft Control Non-Fatal Non-Fatal Single-Engine Tail Strike

C-208 Caravan Non-Fatal Whitewright, TX April 3, 1994

During sport parachute operations the aircraft inadvertently stalled when too many jumpers attached themselves on the outside of the aircraft. The jumpers had been briefed on limiting the number to exit at one time to six; however, they ignored these instructions. As they departed the aircraft the pilot regained control and landed without further incident.

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1994 C-182 Loss of Aircraft Control Non-Fatal Non-Fatal Single-Engine

C-182 Non-Fatal Berea, KY April 2, 1994

The private pilot and four parachutists were on board the airplane as it taxied for takeoff. The wind conditions were reported between 14 and 16 knots. The pilot stated that he added full power, achieved flying speed, rotated, and began to climb out.

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1994 C-182 Fuel Exhaustion Non-Fatal Non-Fatal Single-Engine

C-182 Non-Fatal Nampa, ID February 27, 1994

The aircraft departed fully topped with 65 gallons of fuel on three 45 nautical mile minimum legs plus a total of five parachute drops involving ascents between 7,500 and 9,500 feet above ground level. During the descent from the fifth parachute drop the engine stopped developing power and the pilot in command executed a forced landing in a field. During the landing roll the aircraft collided with a barb wire fence and impacted a drainage ditch.

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1993 C-182 Non-Fatal Non-Fatal Single-Engine Undetermined

C-182 Non-Fatal Woodstock, CT June 13, 1993

The airplane was at 8000 feet, four parachutist had jumped, and the pilot then descended the airplane to the pattern altitude of 1,400 feet. During this descent, carburetor heat was not applied. The pilot then initiated the approach and landing to runway 19. During the approach the pilot applied carburetor heat twice for short periods of time. On final approach the pilot needed additional power to reach the runway.

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1993 C-182 Non-Fatal Non-Fatal Single-Engine Preflight Training

C-182 Non-Fatal Tucson, AZ April 25, 1993

The pilots were completing a parachute/orientation flight. After the parachutists exited, the airplane, with the first pilot at the controls, returned to the airport, descending at the maximum descent rate. The second pilot, a company check pilot, reported that the first pilot touched down simultaneously on the nose and right main landing gears at a high airspeed. The airplane subsequently swerved to the left and struck a bush located about 150 feet from the runway centerline and nosed over.

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1993 C-182 Non-Fatal Non-Fatal Single-Engine Undetermined

C-182 Non-Fatal Washington, OK March 26, 1993

The airplane was being used to haul skydivers. According to the pilot, after about the third or fourth flight, there was a partial loss of power, due to a fuel tank vent that had been blocked by a mud dauber nest. The pilot noted that when a fuel cap was removed, he heard a ‘hiss’ as differential air pressure was relieved. Maintenance was performed to clear the vent, then the pilot continued hauling skydivers.

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1992 C-182 Non-Fatal Non-Fatal Single-Engine Preflight

C-182 Non-Fatal Washington, OK November 27, 1992

A commercial pilot was returning to land after dropping parachutists in the local area. While on short final, the airplane impacted a fence, nosed over, and came to rest in the inverted position. The operator stated that the airplane encountered a downdraft created by a hangar adjacent to the runway. The wind at the nearest observation facility, eight miles north of the site, was from 300 degrees at 6 knots.

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1992 C-182 Non-Fatal Non-Fatal Single-Engine Undetermined

C-182 Non-Fatal Marion, IA October 3, 1992

The pilot stated after the third parachute jumper exited the aircraft, he ‘…Continued at reduced power and started to glide down…For landing. As i was starting a long final approach i saw that i would need power to maintain the glide slope. There was no response when i advanced the throttle.’ attempts to restart the engine were unsuccessful and the pilot made a forced landing. 

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1992 C-182 Non-Fatal Non-Fatal Single-Engine Undetermined

C-182 Non-Fatal Beeville, TX June 6, 1992

During a vfr final approach, following a parachute jumping flight, to a private airstrip the engine lost all power. The pilot made a forced landing into a field. The owner/operator reported that the flaps remained in the up position at the accident site and that the pilot had stated the flaps remained in the up position during the approach and landing. The manufacturers’ procedures list full flaps for a shortfield landing. During the flare/touchdown the nose gear collapsed and the airplane came to rest in an inverted position. The cause of the power loss was not determined.

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