The pilot stated that after four parachutists had boarded the airplane, he began to taxi away from the gate. The pilot stated that the airplane traveled about 25 yards on the upward sloping grass terrain when the right main landing gear collapsed. Examination of the landing gear revealed a break approximately 10 inches from the inboard end of the landing gear leg at a point where it is clamped to the fuselage structure.
Category: Non-Fatal Single-Engine
The pilot stated that the airplane was loaded to the maximum gross weight. He said that on the takeoff roll the airplane did not appear to accelerate, and he anticipated a liftoff speed of 60 to 65 knots. He said he then attempted to stop the airplane; however the brakes locked on the wet grass and the airplane exited the runway at the end and crossed a road before coming to a stop.
The pilot stated that he had refueled the airplane with approximately 3.5 inches of fuel, which equates to 15.5 gallons. According to the Pilot Operator Handbook at 6,500 feet the fuel burn is approximately 13.9 gallons an hour. The pilot flew the airplane for 1.5 hours before the accident. The engine began to run roughly after dropping skydivers and returning to base.
The pilot reported that as the airplane was descending through 4,000 feet msl it started loosing power. She leveled off, pulled carburetor heat on, and switched fuel tanks. She reported that, ‘Upon restart the engine backfired and quit.’ She reported that she trimmed the airplane for best glide (80 mph) and flew directly for the airport 2.5 miles away. At .5 miles from the airport she realized she would not make the runway so she decided to land short.
After three uneventful parachute drop flights with three or four jumpers each, the pilot landed and picked up two jumpers. During the next takeoff roll, the pilot aborted the takeoff and was unable to stop the airplane before it struck a fence at the end of the 2,200 foot asphalt runway. The pilot stated ‘everything was normal, except the plane didn’t lift off.’
The pilot stated he was attempting to land after another airplane which had stopped on the runway. He transmitted three times in an attempt to get the other airplane to expedite off the runway. He then executed a go-around using full power and low pitch. According to the pilot, the engine accelerated briefly, then sputtered, and the propeller began windmilling.
The pilot reported that about 50 feet above the ground after takeoff he began to smell smoke and then saw smoke in the cockpit. He elected to abort the takeoff and land on the runway. He said the airplane bounced once and then landed. After touchdown he steered straight with both brakes full on. When it became apparent that he could not stop before the trees at the end of the runway, he began a hard turn to right.
The pilot was delivering an airplane to a new airstrip. He had been driven to the airstrip to inspect it before the first landing. While landing to the south during the airstrip’s inaugural landing, the pilot lined up to land on the east side of the new runway, and the airplane touched down on an unimproved portion of the airstrip.
The pilot of a tail-wheeled Stearman performed a run-up at the approach end of the runway in the run-up area, and waited for an airplane to land. The pilot then taxied onto runway 31 and began his takeoff roll. A review of a videotape of the accident revealed that the Stearman was right of the runway center line, but its main landing wheels remained on the runway.
After descending from 3,000 feet with engine power off and the carburetor heat on, the pilot entered the traffic pattern to land. While on downwind and base legs the pilot cleared the engine and it responded normally. While on final approach he increased the engine throttle and the engine did not respond.
The pilot descended to land after a paradrop. Entering downwind, he cleared the engine, moved the mixture control to full rich, and applied carburetor heat. Being above traffic pattern altitude he extended his downwind. Upon reaching his base leg, he attempted to add power but the engine failed to respond.
On returning to land, following dropping a load of skydivers, the pilot failed to reset the stabilizer trim and ran out of elevator during the flare for landing. A hard landing occurred and the left main landing gear collapsed causing substantial damage to the underside of the fuselage.
According to the pilot, the flight departed Cook Field uneventfully and attained an altitude of approximately 800 feet above ground level when the airplane experienced a complete loss of engine power. The pilot stated that, ‘the windshield was covered with oil,’ and by looking out the pilot’s side window he was able to land uneventfully in a field.
The pilot stated that he departed for a parachute jump flight with about 25 gallons of fuel aboard the airplane. He said the flight lasted for 30 minutes. When the airplane was on the final approach to the runway, a loss of engine power occurred. The pilot made a forced landing in a corp field adjacent to the airport,
The pilot reported that he had performed a precautionary landing to a corn field due to strong winds, heavy rain, and low fuel. He refueled the airplane and decided to continue to his destination. Initially, the pilot performed a partial takeoff, which was aborted, to obtain the conditions of the field.
The airplane was configured with a single seat, one set of controls, and with seat belts on the floor to haul parachutists. Also, it was loaded to an estimated gross weight of 2,834 lbs; the maximum certificated gross weight was 2,550 lbs. The pilot took off from a soft sod runway (rwy 9) with a crosswind component.
The pilot reported that, before takeoff with the four parachutists, he had checked the flight controls and no evidence of any mechanical problems was noted. During the takeoff roll the airplane accelerated between 60 and 65 mph, became airborne and pitched 60 degrees nose up.
The airplane lost engine power while on final approach for landing, and the pilot performed a forced landing to a unsuitable field which resulted in the airplane coming to rest in the inverted position. The pilot was performing a parachute jumping flight to an altitude of 12,500 feet MSL. During the descent the pilot used carburetor heat, but did not ‘clear’ the airplane’s engine at regular intervals.
The recently employed pilot-in-command (PIC) had been given a 1-hour orientation flight by another pilot the morning of the accident. The airplane used was equipped with only one seat, and the PIC flew the airplane while the pilot who gave the orientation sat on the floor.
The pilot took off with four skydivers on board the airplane, and climbed to 10,000 feet. After the skydivers exited the airplane, the pilot returned to land at the departure airport. The pilot stated that after landing, the airplane impacted parked road grading equipment. He reported that it was a dark night and winds were calm when the accident occurred.
During takeoff for the sport parachute operation, the engine sputtered and quit, and the pilot landed the airplane in a residential yard. Examination revealed that fuel flow through the fuel selector valve was restricted. The fuel selector was disassembled, and the O-rings for the left side were found swelled.
During the landing approach, the pilot realized the airplane was high and ‘started a go around, obtaining partial power.’ When he added additional power, the engine ‘stalled.’ A forced landing was made on the airport. The airplane crossed a taxiway and struck a stockpile of building material. Following the accident, the engine was started and ran ‘normally.’
The airplane was descending after jumpers had departed the airplane in a parachute jumping (skydiving) activity. For the descent, the pilot had reduced the power. When she attempted to increase power, she found that the engine had sustained a total loss of power. During a forced landing, the airplane hit a wire before touchdown, then nosed over in soft terrain.
The pilot carried four parachute jumpers aloft; one left the aircraft at 4,500 feet and the last three left at 12,000 feet. After all the jumpers had exited, the pilot decided to do a power off stall. He stated that he was ‘curious about the gliding abilities of the 182’ and pulled the mixture control to idle cutoff when the aircraft was over the airport at 11,500 feet.
The pilot reported that after parachutists (skydivers) jumped from 13,000 feet, he returned to the airport. While on base leg for landing, two radio-controlled model airplanes were observed flying near the approach end of the runway. The model airplanes swung wide and blocked the first 2,000 feet of the approach end of the runway; thus, moving the available touchdown zone closer to the departure end of the runway.