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1982 C-180 Fuel Exhaustion Non-Fatal Non-Fatal Single-Engine

C-180 Non-Fatal Foyil, OK October 2, 1982

The pilot reported that he had 20 gal of fuel on board when he took off. He climbed to 10,000 ft for a parachute jump, then returned to the airport with an estimated 10 gal of fuel. During a downwind landing, he elected to go around. He said the engine lost power as he was climbing through about 75 ft agl. A forced landing was made in a small pasture. Initially, the mishap was reported as an incident. Before the aircraft was examined, wings had been removed and the aircraft and wings had been transported from the accident site. When examined, both wing tanks were empty, except a small amount of 100 low lead (blue) fuel was found in the right wing tank. Fluid taken from the lines to the left wing tanks had the appearance of automotive fuel. The owner reported that automotive fuel had previously been used. No fuel was found in the carburetor.

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1982 C-182 Loss of Aircraft Control Non-Fatal Non-Fatal Single-Engine Preflight

C-182 Non-Fatal McKinney, TX July 11, 1982

After a normal skydiver drop, the pilot spiraled down for a normal landing on a 2000 ft gravel runway with a powerline at the approach end. The wind was reported as variable at 5 kts. The pilot reported that during the landing, the aircraft touched down on the first 1/3 of the runway and the brakes were applied. Reportedly, the braking action was marginal and the aircraft ran off the end of the runway. The aircraft then struck a ditch and the nose gear failed. Prior to the accident, the pilot was warned that the aircraft brakes were marginal. The density altitude was about 2400 ft.

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1982 C-182 Fuel Exhaustion Non-Fatal Non-Fatal Single-Engine

C-182 Non-Fatal Tuscaloosa, AL June 19, 1982

The pilot had flown from eutaw to seale, al to participate in a parachute activity. Although the plane was equipped for parachuting, it was not used for that purpose on that trip. Before returning to eutaw, the pilot used a dipstick to check the fuel and estimated he had a sufficient amount remaining for the 1.1 hr return flight. He did not check the weather or refuel the aircraft. En route, he encountered clouds, darkness, and heavy rain showers. While deviating from his planned course, he lost track of his position and the fuel supply became low. He diverted to tuscaloosa, al, but ran out of fuel during his approach. The plane struck trees about 1/2 mile from the runway during a forced landing. No seat or seat belt was available for the passenger; however, the passenger received only minor injuries.

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1982 DHC-2 Beaver Loss of Aircraft Control Non-Fatal Non-Fatal Single-Engine

DHC-2 Non-Fatal 15N of Medford, OR May 9, 1982

The pilot started a downwind takeoff on runway 15 with 9 parachutists on board. The runway was unidirectional requiring takeoffs on runway 15 which sloped downhill. After beginning the takeoff roll, the pilot had difficulity in maintaining directional control and initiated abort procedures. Reportedly, the aircraft continued to veer to the right in spite of the use of hard left rudder and braking action. As the aircraft decelerated, it departed the right side of the runway, struck 3 fence posts, and collided with a parked stinson, n368c. The pilot reported that the parachutist occupying the copilot’s seat stated that he had placed his feet behind the rudder pedals shortly before takeoff.

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1982 C-182 Fuel Exhaustion Non-Fatal Non-Fatal Single-Engine

C-182 Non-Fatal Quincy, FL April 4, 1982

After completing the drop on a skydiving flight, the engine lost power during a power-off descent. The pilot reported that the carburetor heat was not used during the descent prior to the loss of power. However, the probability of weather conditions for carburetor ice was not verified. The aircraft struck a fence during an off-airport landing, before reaching the runway. The pilot reported that he took off with 10 gallons of fuel on board. The plane crashed about 15 minutes after takeoff. An examination of the engine revealed no malfunction or failure prior to the accident.

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1982 C-182 Loss of Aircraft Control Non-Fatal Non-Fatal Single-Engine

C-182 Non-Fatal Midland, NC March 17, 1982

The pilot reported landing on a soft, slick runway at dusk after returning from a parachute jumping mission. The aircraft was landed off of the center of the runway and veered left in soft terrain. The nosewheel sank in mud as the plane crossed a shallow ditch and flipped over.

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1982 C-182 Non-Fatal Non-Fatal Single-Engine Severity Undetermined

C-182 Non-Fatal Woodland, CA March 6, 1982

A climb was made to 10,000 ft on a skydiving flight. The pilot reported that after descending to 2000 ft, the engine began to lose power and run rough. He elected to make an off-airport landing in a field. Near the end of the landing roll, the nose gear sank into soft terrain, and the aircraft flipped over.

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