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2017 AL Ferry Fuel Exhaustion Harvest Non-Fatal Non-Fatal Single-Engine PAC 750XL Preflight

PAC 750 Non-Fatal Harvest, AL August 28, 2017

The commercial pilot was conducting a cross-country flight to deliver the airplane to a maintenance
facility. The airplane departed with full fuel tanks. The pilot stated that, as the airplane neared the
planned fuel stop airport, he thought that there was adequate fuel remaining to reach the maintenance
facility, so he did not stop to refuel and continued to the destination. About 4 hours 23 minutes into the
flight, which was past the expected fuel exhaustion time of about 4 hours 18 minutes (assuming a fuel
burn of 50 gallons per hour, which the pilot used for his initial flight planning), the pilot declared an
emergency and advised an air traffic controller that the airplane was out of fuel. The controller provided
information to the pilot about nearby airports, but the airplane would not have been able to reach any of
them, so the pilot initiated a forced landing to a field. Before touchdown in the field, the pilot descended
to avoid power lines ahead, but the airplane hit one of the lines. The airplane touched down in the field,
impacted an embankment, and came to rest upright on a road. The airplane sustained substantial
damage.

Read the NTSB report.

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2016 Collisions Other Non-Fatal Single-Engine PAC 750XL Training VA Warrenton

PAC-750 Non-Fatal Warrenton, VA September 9, 2016

The pilot reported that this was his third skydiving flight of the day and he performed a back taxi on the
runway for takeoff. He further reported that as he rotated the airplane for takeoff, he heard a “steady”
stall warning horn, the flight controls felt mushy, and the airplane would not climb. The pilot reported
that he aborted the takeoff and applied max braking and reverse thrust, but the airplane overran the
runway remaining. Subsequently, the landing gear collapsed and the airplane collided with a fence.

Read the NTSB report.

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2015 NC Non-Fatal Non-Fatal Single-Engine PAC 750XL Raeford

PAC-750XL Non-Fatal Raeford, NC December 03, 2015

The commercial pilot of the single-engine turboprop airplane reported that he was preparing to release
skydivers when he noticed that the engine torque indication was in the red arc. Specifically, the gauge
was indicating a torque of 70 pounds per square inch (psi) when it should have been indicating about 25
psi; the maximum allowed torque indication was 64.5 psi. The skydivers jumped uneventfully. As the
pilot was returning to the airport, the torque gauge was indicating 80 psi while the engine was at idle. At
that time, the pilot decided to perform a precautionary engine shutdown and land with no engine power.
During the landing, the airplane was fast and touched down about halfway down the 3,402-ft-long
asphalt runway. The pilot applied heavy braking, but the airplane traveled about 1,000 ft beyond the
departure end of the runway before coming to rest upright in a field with a collapsed left main landing
gear.

Read the NTSB report…

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2014 Mechanical Failure Non-Fatal Non-Fatal Single-Engine PAC 750XL VA Warrenton

PAC 750XL Non-Fatal Warrenton, VA May 09, 2014

According to the commercial pilot, following a skydiving operation, he returned to the airport. During
the landing attempt and as the airplane was about 15 ft above ground level, the airplane banked left and
the left main landing gear (MLG) then contacted the turf runway, so he immediately performed a goaround.
Ground personnel subsequently contacted the pilot via radio to inform him that the left MLG
had separated from the airplane. The pilot then performed an emergency landing, and, during the landing
roll, the left wing contacted the runway, which resulted in substantial damage to the left wing spar.

Read the NTSB report